After a couple of weeks delay in Hayward (see below) Rob Leach departed Oakland for Honolulu on the morning of Sunday, June 18. He arrived in Honolulu about 14 hours later. The flight was uneventful except for the rear (#2) alternator failing.
The compression was checked in Honolulu and found to be excellent. The alternator was checked and found to be OK - the fault is apparently some intermittent fault or adjustment required in the master control unit. This will be investigated later. For now, cycling the alternator seems to fix it.
Rob flew Honolulu to Christmas Island on Wednesday. The flight was long, 8 hours, but uneventful. Next leg is to Pago Pago.
On 25th June, 2000, N142CD landed at Archerfield airport, at around 4pm local time. A crowd of about 30 people were waiting, and champagne was broken out to celebrate.
| KDLH | Duluth | |
| KPIR | Pierre | 370 nm |
| KPUB | Pueblo | 412 nm |
| KCYS | Cheyenne | 173 nm |
| KOGD | Ogden | 325 nm |
| KLWL | Wells | 132 nm |
| KHWD | Hayward | 393 nm |
| KOAK | Oakland | 6 nm |
| PHNL | Honolulu | 2089 nm |
| PLCH | Christmas Island | 1161 nm |
| NSTU | Pago Pago | 1261 nm |
| YSNF | Norfolk Island | 1477 nm |
| YBBN | Brisbane | 789 nm |
| YBAF | Archerfield | 13 nm |
The major delay was due to engine problems; a compression check revealed 4 cylinders with low compression (3 with very low). Three cylinders were removed and sent to Teledyne Continental Motors for inspection. They reported that the cylinders were undamaged, but had fuel deposits in the valve seats. They authorized fitting three new cylinders.
Unhappy with this result, we arranged for inspection of the other three cylinders by a third party. This showed that the cylinders had been overheated and the valves burnt. TCM then, with Cirrus Design's encouragement and assistance, provided a new engine. This was fitted, then inspected by a Cirrus Design technician, and test flown by a Cirrus factory pilot, with very satisfactory results (all cylinders show excellent compression).
The exact cause of the engine problems is not yet clear, except that at some point in its (short) history, it appears to have been operated at high power and lean mixture. No possible explanation has yet been identified.